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Re: Brass Ball static spark gap not doing so well
Original poster: "by way of Terry Fritz <twftesla-at-qwest-dot-net>" <Tesla729-at-cs-dot-com>
In a message dated 5/27/01 2:24:39 PM Central Daylight Time, tesla-at-pupman-dot-com
writes:
>
> I want to piggyback on what Deano said. I've also had
> bad pitting problems with brass, so I dumped it in
> favor of copper, which seems much more durable.
> However, I did use 1/4" treaded brass rod for my
> Asynch RSG, and it worked out pretty well. The brass
> still evaporates away, but the rod is too small
> diameter to exhibit any pitting. Instead, the entire
> rod tip slowly eats away. When the gap finally gets
> too wide due to erosion, I simply re-gap, and I'm good
> to go for a few more weeks. This is just for the
> fixed electrodes. I've never had to service the
> flying electrodes, which are made of the same brass
> rod material.
>
> Greg
> http://hot-streamer-dot-com/greg
Hi Greg, all,
I have had pretty much the same experience with threaded brass
rod electrodes. With my 10 kVA pig driven system, I use 1/2" dia
threaded brass rod for the stationary electrodes and 3/8" dia
threaded brass rods for the flying electrodes (asynch -at- ~ 300 bps)
With these larger diameter rods, erosion is quite minimal. BTW,
there are twin rotary discs, each with 6 flying elctrodes, which are
in series, so there are a total of 4 SGs. The one disadvantage of
the larger flying electrodes is that -at- 3/8" X 2" long, plus two fitting
SS nuts and wahers with each brass electrode, they are rather
heavy and it takes the 1/3 HP, 3450 RPM bench grinder motor
several seconds to bring the RSG up to operational speed after
power up.
Sparkin' in Memphis,
David Rieben